Resolved KTM X-Bow with Direct Drive

Discussion in 'Community Support' started by Lachaussette, Aug 21, 2017.

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  1. Lachaussette

    Lachaussette Well-Known Member

    Joined:
    Jan 29, 2015
    Ratings:
    +352 / 0 / -0
    Hello,

    Since I have my RFR Wheel basing on MIGE 130ST-M10010 with encoder 10000ppr (it's an expensive but really nice upgrade of my materials) I have a problem only with the KTM X-Bow, it send me back a strange FFB. While all other models of cars are totally fluid in the steering wheel as it would be, the KTM has a granular direction, unpleasant vibrations not due to track effects while my mmos is correctly managed and while everything works perfectly with the other cars.

    Friends which have exactly the same steering wheel don't have this problem and settings are configured in the same way.

    I don't understand the problem...any idea? I point out that the parameter "minimal intensity of FFB" is setting on 0 value.

    Thanks ;)
     
  2. Lachaussette

    Lachaussette Well-Known Member

    Joined:
    Jan 29, 2015
    Ratings:
    +352 / 0 / -0
    Resolved : I didn't change the FFB multiplier after changing my TS-PC for the DD. Setting for TS-PC was 4500 (OMG!) and for DD setting between 1500-1800 is better.